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Mishaps
- To have your mishaps included in the website, simply email the author!
Please carry a camera in your car!!
There
have been several mishaps latery. Here are just a few pictures of accidents
that were almost all avoidable.
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Early
Summer 2003: The Harlow club decided to demonstrate some low flying.
All went well for some time. Lower and lower. Down the valley, over
the wood, hugging the hills at 5 feet. Then a power dive from about
500 feet. The magnum held it fine. At about 190 mph the hill jumped
up 3 feet and bit the magnum! Spectacular. Bits everywhere, they decided
to warm up a bit,,,,
Early
August 2002: Richard From the Stansted club suffered a structural failure
while trying out a new engine. Had been happily flying round when a
horrendous crack was heard. The tail section was seen fluttering down
and the front ploughed flat out into the newly 'ploughed' field! What
a mess. Sorry Richard. We don't like to see all that hard work ending
in disaster. For research and development and gluing knowledge only,
you can view the wreckage!
Mid
August 2002: Chris from the Stumps Cross club lost his brand new model
(Well I was actually flying it! I was trying it out before giving him
a lesson!) Anyway, not sure what actually happened. Could have been
the first case of radio interference at the site. I was coming across
the site from right to left level with the ditch. At about 40 feet,
the model seemed to go elevator down, by its self. I pulled full back
elevator and it recovered a little then went full elevator down! It
went flat out into the ditch at about 70 mph. Not a lot left. The engine
was buried, the servos were all damaged and the fuselage was unrecogniseable.
Sorry Chris!!!! We have still not found out what happened.
7th
April 2001: Gary (Website author!) Lost his trusty model the 'Bitza'
which John (and Boo Boo) Wilkins from Linton built about seven years
ago. I was larking about with John McLaren pulling loop after loop when
after about a 15 minute flight it decided to carry on in a straight
line. Unfortunately the line was directly towards the Eastern field.
After
pulling out the engine and fetching a carrier bag, the model was taken
home for accident investigation. It is one thing loosing a model, but
it is another thing if the reason is not known. I discovered that although
the battery had been completely charged on the field charger and showed
a voltage of six volts on the meter, after only 15 minutes, the voltage
had dropped to 4.3 volts. Everything still worked with the radio up
close, when the radio was moved a few hundred feet away, it went out
of range. The battery was probably over 10 years old. When should I
have thrown it away??!!!
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